SAVAGE
Member
- Location
- Richfield Utah
I'm swapping a cummins into a 1988 GMC 1 ton crew cab dually. Im also converting it to single rear wheel. However i'm already halfway through this project so Ill help get you caught up. I had my eye on a old gmc that belonged to a rancher friend of mine. I asked if he would consider selling it to me and he told me that with all the work I had done over the years if I wanted the truck it I could have it.
This is how we found the old girl. 85,000 original miles, not a dent on her.
View attachment 0801001233.jpg
We where lucky the trailer was big enough.
View attachment 0803001749.jpg
Well we got it pushed in the shop and after a month of figuring out why she wouldn't run we found out the exhaust was plugged with a bunch of dead mice/mouse crap/nest crap. We saw the exhaust off and it fired right up. And of course we wheeled it...a little.
Next I put on some 265 75 r-16's, 4" lift, headers and painted a few things black for extra coolness... and wheeled it a little more.
View attachment 1110001652.jpgView attachment 1121001153.jpg
Then it sat in the yard for two years while I was preachin the good word. When I got back I was plagued with 454 TBI issues. I couldn't figure out why it never had much power, idled crappy, sputtered, stalled, and all that goes with it. I tinkered with it as time would allow trouble shooting everything I could think of. Turned out to be the little 1.5" piece of rubber hose in the sending unit between the fuel pump and the metal tube had a small crack relieving fuel back into the tank resulting in a significant loss of pressure to the throttle body. I was a fool and ruled out that possibility because it ran the same on both tanks. Well both sides had the same problem. Major pita.
This is how we found the old girl. 85,000 original miles, not a dent on her.
View attachment 0801001233.jpg
We where lucky the trailer was big enough.
View attachment 0803001749.jpg
Well we got it pushed in the shop and after a month of figuring out why she wouldn't run we found out the exhaust was plugged with a bunch of dead mice/mouse crap/nest crap. We saw the exhaust off and it fired right up. And of course we wheeled it...a little.
Next I put on some 265 75 r-16's, 4" lift, headers and painted a few things black for extra coolness... and wheeled it a little more.
View attachment 1110001652.jpgView attachment 1121001153.jpg
Then it sat in the yard for two years while I was preachin the good word. When I got back I was plagued with 454 TBI issues. I couldn't figure out why it never had much power, idled crappy, sputtered, stalled, and all that goes with it. I tinkered with it as time would allow trouble shooting everything I could think of. Turned out to be the little 1.5" piece of rubber hose in the sending unit between the fuel pump and the metal tube had a small crack relieving fuel back into the tank resulting in a significant loss of pressure to the throttle body. I was a fool and ruled out that possibility because it ran the same on both tanks. Well both sides had the same problem. Major pita.