I love itThis is what those bolts became. Bored out a pocket in the face of a hockeypuck to make industrial adjustable table feet.
View attachment 134444View attachment 134445
I love itThis is what those bolts became. Bored out a pocket in the face of a hockeypuck to make industrial adjustable table feet.
View attachment 134444View attachment 134445
you should check out the bump stop pads on my XJHockey pucks are super useful and pretty cheap 😎
If vinyl gates were made this way by the fence people, they might actually justify the prices they charge for them. I cannot believe how flimsy, crappy, unpainted, and generally shitty they are for the cubic dollars. Yours looks SO MUCH better.Since we had to start over on the gate we opted to incorporate some "kustom" touches for improving the design and definitely to extend the life. Saturday I got to hang out with my son in the shop so it was a good day.
We opted to machine some items to allow us to bolt the last section together on the gate vs. the entire thing being fully welded. It should be easier to assemble after paint and hold up much longer.
Machined and threaded a block to receive the end piece.
Added a little extra thickness to the end of the tubing to prevent breaking out like the last one.
Drilled a hole through the leg to allow the use of a socket head cap screw to secure everything together.
The ID of the wheel was 1/2" but very sloppy. We also wanted to use something larger than .5" rod as the axle so I drilled out the wheel to .625" and then used an appropriate rod.
Single point threading 1/2"-13 threads so allow the rod to thread into the other leg.
Machined another block but this one threaded to 1/2"-13 to receive the axle.
Opposite side beefed up like the previous one but a .625" recess machined to a depth of .125" which will allow the .625" axle to sit in for extra rigidity.
Axle completed with one end threaded and the other drilled & tapped to receive a 3/8"-16 socket head cap screw.
Axle test fitting.
Wheel test fit.
Bolted together and just enough clearance to allow the wheel to turn freely but with much less "wobble".
Clamped to the welding table to true up and weld.
Fabrication completed.
All that’s left is to prime & paint it then assemble the vinyl before reinstalling it.
Mike
If vinyl gates were made this way by the fence people, they might actually justify the prices they charge for them. I cannot believe how flimsy, crappy, unpainted, and generally shitty they are for the cubic dollars. Yours looks SO MUCH better.
That truck looks to be in amazing shape! Hard to believe it's a '96.Monday night I made a little headway on the 1996 Dodge 2500 V10.
Removed the battery cables.
They’re in pretty bad shape. Lots of green crusties on both.
Then moved on to brakes. Started by pulling all the tires & wheels.
Leaking axle seal.
Disassembling.
Hub removed.
Hub bearings & seal disassembled and cleaned.
I was able to compile a list of parts in which I picked up the next day.
Mike
I have two gates that I'll be rebuilding this spring. I put in wider gates last summer and the old ones are going to be repurposed. I don't think my work will even compare to yours but it was great to see what you did. As @I Lean said, if built like yours, they'd be worth the price they charge.Since we had to start over on the gate we opted to incorporate some "kustom" touches for improving the design and definitely to extend the life. Saturday I got to hang out with my son in the shop so it was a good day.
We opted to machine some items to allow us to bolt the last section together on the gate vs. the entire thing being fully welded. It should be easier to assemble after paint and hold up much longer.
Machined and threaded a block to receive the end piece.
Added a little extra thickness to the end of the tubing to prevent breaking out like the last one.
Drilled a hole through the leg to allow the use of a socket head cap screw to secure everything together.
The ID of the wheel was 1/2" but very sloppy. We also wanted to use something larger than .5" rod as the axle so I drilled out the wheel to .625" and then used an appropriate rod.
Single point threading 1/2"-13 threads so allow the rod to thread into the other leg.
Machined another block but this one threaded to 1/2"-13 to receive the axle.
Opposite side beefed up like the previous one but a .625" recess machined to a depth of .125" which will allow the .625" axle to sit in for extra rigidity.
Axle completed with one end threaded and the other drilled & tapped to receive a 3/8"-16 socket head cap screw.
Axle test fitting.
Wheel test fit.
Bolted together and just enough clearance to allow the wheel to turn freely but with much less "wobble".
Clamped to the welding table to true up and weld.
Fabrication completed.
All that’s left is to prime & paint it then assemble the vinyl before reinstalling it.
Mike
That truck looks to be in amazing shape! Hard to believe it's a '96.
I have two gates that I'll be rebuilding this spring. I put in wider gates last summer and the old ones are going to be repurposed. I don't think my work will even compare to yours but it was great to see what you did. As @I Lean said, if built like yours, they'd be worth the price they charge.
...maybe “table bases and coffee” meets should be a thing. 🤔🤷♂️They don’t call you Kitchen Table Ryan for nothin’
the only chunk of 8" square tube I could find was 1/2" thick so I would guess the base alone weighs 125 Lbs. 2 guys can pretty easily get in and out of the bed of the truck.for real stability, fill the center void with concrete