Here's the updates for it.
Well she's up and moving! Here's some small and large details on how it went down :
So being it's a heat pumping big block and stuff is close I've been wrapping alot of stuff in heat protection Like water lines, wires, etc. Samples :
Eventually I want to pull the headers off and have them ceramic coated for heat and life prolonging.
Then I finished up some other electrical things like wiring the rear end for rocklights, tail lights, reverse light, winch, kill switch fans, return to center module, other stuff too.
So then some not so fun stuff. Got the drivetrain, driveline etc in right? Transmission shifter adjusted, everything spins, engages nicely, fluids topped off...yet no movement...trans was obviously spinning, confirmed by the sound of the park pin grinding on the output when put into park
Turns out after much examination and phone calls to parts manufacturers we had the wrong output in the trans. It was 2 1/8" short. Luckily our trans guy had the correct one, a 9 1/8" total length output style. We had to rip everything out and take the trans back apart.
Got it gutted, annoyed our transmission guy by staying there and watching/talking to him, and Bam! Splines are actually going together and the trans worked flawless.
So after a couple test runs here how it ended:
First run - fuel issue, running hot issue, miss fires
Second run - less fuel issue, still hot, still misfires. Also noticed front end didn't steer as sharp as the rear.
Third run - even less fuel issue, not running as hot, only misfired/backfire when hot, leaking motor oil from all around the oil pan.
Fourth run - fuel issue fixed, oil pan fixed heat issue figured out.
So what happened here is the first run was just putting around getting a feel for it. Was coughing and choking out, but when it caught up it actually got up and scooted. Turns out these issues was a mix of low fuel flow and two melted spark plug wires on the headers through the heat boots. Got the plug wires fixed and figured the fuel issue was we put in to fine of a fuel filter mesh. Went from 100 microns to 40s and fuel/throttle is great! We've narrowed down the heat issue to being the fans on the radiator just don't pull enough and seem to slow down when they get warm. Gonna solve this with two Taurus fans. The oil pan leaked turned out to be part of my gasket was blown out. Fixed it by switching from moroso full rubber back to a felpro 4 piece cork/rubber/silicone. Also addressed the steering issue, all it was is the steering stops were adjusted different. Made them match the rears stops and it's much much better